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Type: Posts; User: mcparker

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    I am confused then why would the same system work...

    I am confused then why would the same system work with the native bit resolution and faster pulse speed?
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    I removed the L298N from the system and drove the...

    I removed the L298N from the system and drove the motors straight from the Teensy pins (goal of a 20kHz drive frequency). I used the 24 Mhz CPU speed with 10 bit resolution with an ideal frequency of...
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    16583 2 x DC Motors connected thru an...

    16583

    2 x DC Motors connected thru an H-Bridge on two encoders with a 12 V DC power supply.

    The rest of the wires are for the buttons and display.

    Thank you for the help.
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    Issue with analogWriteResolutoin

    I posted the original code and I have still having issues getting analogWriteResolution. In the code below, if I change the PWM or drive Frequency off of the ideal for the Teensy 3.6 CPU the motors...
  5. Is there a reason whenever I try and change the...

    Is there a reason whenever I try and change the resolution to anything other than 8 Bit, like analogWriteResolution(11); //11 Bit with the corresponding change in the resolution range, the signal...
  6. Thanks. I will correct my math and let you know. ...

    Thanks. I will correct my math and let you know.

    Is there an updated chip that I should use to improve the performance?
  7. Yes. I am trying to send the PWM to the HBridge....

    Yes. I am trying to send the PWM to the HBridge. The reason for the higher frequency is that I am trying to match the frequency of the production MCU/PCB which is 20 kHz signal.

    The default...
  8. Issues with analogWriteResolution() and analogWriteFrequency() Teensy 3.6

    Hey ya'll,
    I am an ME trying to emulate the main PCB drive signal for motor testing. I am using a Teensy 3.6 + L298N Dual H Bridge + DC Power supply to power strings of 12V DC Motors.
    The code...
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